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Fab Eliminates Yield Loss due to Manual Wafer Handling

 Wafer scratches can significantly contribute to probe yield loss in mature fabs.

Laura Peters, Senior Editor -- Semiconductor International, 6/1/1998

A mature fab known for low cost, low cycle time manufacturing can suffer significant yield loss because of a number of manual wafer handling procedures. Texas Instruments (TI, Dallas, Texas) was able to automate wafer handling in a mature fab that was experiencing a 7% yield loss that was due to wafer scratches caused by manual handling. The company effectively eliminated manual handling in the photolithography and plasma areas of the fab, reducing resist-related scratches by 83%. The improvements in yield helped fund the second and third phases of the program, automating wafer handling throughout the fab.

TI first estimated yield loss that was due to manual wafer handling by determining the average number of new scratches at each of eight inspection steps in the process. When physical defects on wafers were detected and analyzed, a 7% yield loss was estimated. Approximately 95% of the scratches were randomly located on the wafers, indicating that the vast majority were caused by human error and not equipment-related problems. By tabulating each manual transfer of a wafer, the group found that a total of 535 individual manual wafer transfers took place per lot, averaging 22 wafer handling procedures per wafer. Using an average of 3% die affected per scratch, a 7% yield loss was confirmed. By categorizing the scratches by type of handling performed (Fig. 1), TI determined that the highest percentage was performed in verifying lot numbers on the wafers (28%). When broken out by fab area, 51% of the handling took place in the critical photolithography and plasma processing sections, which were then selected for the first phase of automation.

The company formed quality improvement teams (QITs), each consisting of 10-15 people to address automation of the photo and plasma areas on each of the fab's three shifts per day and A and B shifts on the weekends. Comprised largely of manufacturing

06YM1A

Fig. 1. Twenty-eight percent of handling steps were performed to verify lot numbers on the wafers.

operators, supervisors and equipment maintenance technicians, the QIT members listed manual handing operations in their respective areas and brainstormed ways to eliminate handling steps. They then tested the alternatives to determine the most production-worthy solutions. To improve lot verification steps, for instance, the personnel changed procedures to always load wafers in cassettes with flats (and therefore scribed numbers) located on the top for easy visibility. Small flashlights and additional flat finders were installed at the workstations.

Another example involved the handling of wafers in and out of a batch metal etch tool with special leading requirements. Pilot wafers are typically added to round batch sizes to 12, 16 or 18 wafers. Special steps are also required for particle monitoring and statistical process control (SPC), reactor conditioning and endpoint checks following maintenance. A four-cassette wafer sorter was used to accommodate these complex recipe changes. Throughout the course of the project, unnecessary wafer handling procedures were eliminated either by restructuring the process, or by making process and equipment enhancements suggested by yield enhancement or process engineers and technicians.

To measure the success of the project, the QITs tracked the number of vacuum pencils removed from the fab twice a month and the average number of scratches detected each month. Scratches were categorized by resist scratches, in which a feature was disturbed by resist fragments before etching, which subsequently blocked the etch, and non-resist scratches, in which debris blocks the etch. After implementing phase-1 actions, resist-related scratches were reduced by 83% (Fig. 2).

06YM2A

Fig. 2. By replacing manual with automated wafer handling and optimizing procedures, resist-related scratches were reduced by 83%.

The program also delivered unanticipated benefits by uncovering procedural inefficiencies. For example, the stepper wafer-handling robot positioned setup wafers on a wafer pedestal for retrieval with a vacuum pencil. The pedestal was replaced with a short cassette that could fit on the CD-SEM and be returned to the stepper. Inefficient automatic wafer handlers were identified and fixed or replaced. In addition, manual assists that were not previously tracked were now identified using a software tool that recorded "production" vs. "manufacturing maintenance" time on each of the tools. In this way, the assists were systematically prioritized, and 85% of the root causes were eliminated within three months.

The results of this project were reported by Richard Guldi, et al., in the 1997 proceedings of the IEEE/SEMI Advanced Semiconductor Manufacturing Conference.

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